> Anyhow, multiple flights later the motor quits. Inspecting the motor and
> testing the ESC shows the motor is burnt out.
>
> Question 4: Why would the motor burn out? Yes, I was doing some full
> throttle runs whilst towing a small glider (Alula under 400grams) which it
> handles with ease.
> Question 5: The HiMark motors are very good and fit the plane perfectly.
> Should I fit another and be a little cautious on throttle application and
> duration?

Signature
Tim Wescott
Wescott Design Services
http://www.wescottdesign.com
Do you need to implement control loops in software?
"Applied Control Theory for Embedded Systems" was written for you.
See details at http://www.wescottdesign.com/actfes/actfes.html
>> I have a Multiplex MiniMag which I've been flying for some time with the
>> following setup:
[quoted text clipped - 26 lines]
> electrical engineer knows that a meter must be built with care to measure
> correctly under such conditions.
I realise not all E-meters are the same but I doubt they'd be out that much,
noting the 25A ESC didn't complain at all.
> So it could just be the meter. In particular, if the meter was measuring
> the instantaneous current to the motor (see my answer to question 3,
> below).
WOT static run, not an instanteous peak.
> Also, one 8x6 isn't necessarily like every other 8x6 in the world.
True, but all props were the same brand and type.
> I very much doubt this is the case, but if you switched a 7x5 with really
> fat blades for an 8x6 with skinny blades the power could drop. I really,
> really doubt that this is the case, and certainly isn't if you chose a
> prop that was generally similar, just bigger in every way.
7x5E APC and 8x6E APC. PCPhill is suggesting these may be too big, and is
probably right. However, I couldn't get anyone at a hobby shop or the flying
field suggesting I go smaller. They all said bigger equalled less Amps -
which can only be true if the RPMs drop. I'm no e-flight guru but I know
enough engineering to understand that increasing load (at any revs) will
also up the Amp draw (at those revs).
> Do you happen to know if it went slower with the 8x6?
We missed that on the e-meter with the 7x5E. All I can say is the 8x6E was
pulling 11000RPM static.
> I think that if you've found out anything the least bit startling with
> your meter vs. prop test, it's that the meter isn't reading what you think
> it is.
What's the efficiency ratings of ESCs like? Are some 'horrible' and others
reasonable? Perhaps the Turnigy ESC is highly inefficient compared to the
Castle Creations.
>> Question 2: Why would a 40A ESC deliver more than 50A (static) without
>> getting hot or cutting out? It doesn't make sense.
>
> A well-engineered piece of equipment will always take more than the label
> says. I would expect some heating if the current measurement is accurate,
> however.
Neither ESC got hot (once proper airflow was established).
>> Question 3: Why would a 25A ESC run perfectly if there is a 50A draw?
>
[quoted text clipped - 4 lines]
> be what the ESC can stand. If it's limiting the _average_ current, then
> the instantaneous _peak_ current would go up to 50A easily.
Perhaps the Castle Creations do limit max current draw and the Turnigy
doesn't.
> Note also that a bigger prop may raise the instantaneous current without
> changing the average current.
[quoted text clipped - 10 lines]
> 40 (or doesn't limit at all), then that would explain it. Or if you
> switched to the 8x6 prop based on an erroneous current reading.
I'm starting to believe that.
>> Question 5: The HiMark motors are very good and fit the plane perfectly.
>> Should I fit another and be a little cautious on throttle application and
[quoted text clipped - 24 lines]
> Or just buy a big pile of motors, and do stunts as soon as you see a smoke
> trail.
If I could get a HobbyCity motor with the same mounting screw spacing (16mm)
then I'd be buying a few of those.
Regards
Tim Wescott - 08 Jul 2010 18:30 GMT
>>> I have a Multiplex MiniMag which I've been flying for some time with the
>>> following setup:
[quoted text clipped - 29 lines]
> I realise not all E-meters are the same but I doubt they'd be out that much,
> noting the 25A ESC didn't complain at all.
Obviously you haven't designed products with a sales guy hovering over
you, trying to push things into production when you know they're still crap.
>> So it could just be the meter. In particular, if the meter was measuring
>> the instantaneous current to the motor (see my answer to question 3,
>> below).
>
> WOT static run, not an instanteous peak.
Instantaneous = instantaneous. An ESC pulses the current to the motor
(that's why it makes all those chirpy-whiny sounds), and the motor
current takes microseconds or milliseconds to respond to the motor
voltage. Meters read over seconds; to see what's happening with the
winding current you need an oscilliscope, and you need to look at things
in the microsecond or millisecond range.
If the meter reads the peak current instead of the average, or if the
meter samples the instantaneous current and pretends that it's average,
you'll get all sorts of confusing results.
>> Also, one 8x6 isn't necessarily like every other 8x6 in the world.
>
> True, but all props were the same brand and type.
Then that's not it.
>> I very much doubt this is the case, but if you switched a 7x5 with really
>> fat blades for an 8x6 with skinny blades the power could drop. I really,
[quoted text clipped - 7 lines]
> enough engineering to understand that increasing load (at any revs) will
> also up the Amp draw (at those revs).
You're right, they're confused. There's more than one way to drive a
motor, but the way that ESCs drive brushless motors makes them 'want' to
turn at a constant speed, and as they slow down they'll draw more
current to produce more torque. The two easy limits to this are to
imagine the motor with no prop at all, and imagine the motor with the
shaft glued to the case. With no prop the motor will only need to pull
enough current to overcome mechanical friction and electrical losses.
With the shaft glued to the case the motor can't turn at all, and the
current is limited only by the winding resistance and the ESC.
>> Do you happen to know if it went slower with the 8x6?
>
[quoted text clipped - 8 lines]
> reasonable? Perhaps the Turnigy ESC is highly inefficient compared to the
> Castle Creations.
Based on my modest experience designing switching amplifiers, and my
extensive experience hanging out with designers of switching amplifiers,
you should expect efficiencies ranging from 80% to 98%. Based on price
tags and Castle's reputation I would expect they're above 95%. I don't
know Turnigy, but I doubt they beat out Castle.
When a switching amplifier (which is the "business end" of an ESC) is
inefficient, all the power lost in the amplifier turns into heat -- so a
less efficient ESC is a hot ESC.
>>> Question 2: Why would a 40A ESC deliver more than 50A (static) without
>>> getting hot or cutting out? It doesn't make sense.
[quoted text clipped - 4 lines]
>
> Neither ESC got hot (once proper airflow was established).
So there was some heating, which you controlled with proper airflow.
>>> Question 3: Why would a 25A ESC run perfectly if there is a 50A draw?
>>
[quoted text clipped - 7 lines]
> Perhaps the Castle Creations do limit max current draw and the Turnigy
> doesn't.
Certainly that's more likely than the other way around.
>> Note also that a bigger prop may raise the instantaneous current without
>> changing the average current.
[quoted text clipped - 46 lines]
>
> Regards

Signature
Tim Wescott
Wescott Design Services
http://www.wescottdesign.com
Do you need to implement control loops in software?
"Applied Control Theory for Embedded Systems" was written for you.
See details at http://www.wescottdesign.com/actfes/actfes.html