> Dave,
>
> Try a new set of crystals first, if they are the same ones (esp RX end) that
> were in the crash it might have fractured also check for binding in linkages
> anywhere which could be stalling a servo and dragging the supply voltage
> down to unusable levels.
Excellent points. The receiver did come with a new
crystal, so I guess that rules that out. I've looked
for binding, etc., but everything seems to be ok.
I've monitored the on-board VoltWatch and see no dip
in voltage as controls are moved about.
Also as you have fitted a brand new rx battery
> pack, cycle it a few times to make certain it does not have any duff cells
> and is producing its best voltage. Nimh cells are notorious for not giving
> full voltage/capacity for the first couple of cycles or failing early in
> life. I have seen two new NiMH packs with dead/dying cells in the last 6
> months that were initially put down as radio interference.
I built up the new rx pack with 4 new Sanyo KR-1500
nicads and then cycled them with my AccuCycle several
times before commiting to flight. Capacity seems good.
All connecting wires and plugs are also new.
I suppose there could be an intermittant bad cell, but
the glitches are so consistant with what happened with
the old flight system and battery pack that I'm left
wondering what's left to replace on/in the helicopter.
Maybe something metal-to-metal I haven't yet discovered
or a noisy ball bearing... maybe I should just buy a
new heli :-)
Thanks for your reply!
Dave
Chris Dugan - 28 Jun 2004 21:46 GMT
> dstaffor[SpamNot]" <"dstaffor[SpamNot]"@calpoly.edu> wrote in message
news:cbpi20$4eu$1@cscnews.csc.calpoly.edu...
> > Dave,
> >
[quoted text clipped - 33 lines]
>
> Dave
OK not much left then apart from belt static such as affects some other
helis, try earthing the boom to the engine mount somewhere. This is usually
only a problem on electric heli's but has been known to affect glow ones as
well. You could also try spraying some silicone spray on the belt and
pulleys to see if that cuts down on static that's a quick thing to try
before drilling holes in the boom to mount an earth wire.
Was the glitch accompanied by a change in the engine note? if so it might be
worthwhile flushing the carb and tank out incase there is any debris inside
causing a brief lean burst and accompanying brief increase in power.
Chris
Stickman - 28 Jun 2004 22:22 GMT
Something else worth trying if possible is change the RX. Futaba Dual
conversion RX's had a problem with a ceramic filter getting damaged in a
bump. The RX would appear to work but would glitch in the manner that you
describe.
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